cupofjoe_84
Member
After letting the warrior warm up with stock 42.5 pilot jet, I tried turning it out and it got better the more I turned out. 4 turns out and I could blip the throttle pretty well, so I tried a bigger jet, 45. With that in, it idles way too high adjustments to the mixture screw do nothing. The screw that turns throttle higher is turned all the way out by the way so that is not the problem. I have tried the carb cleaner trick and cannot find any air leaks. I have a k&n like air filter and a D&G exhaust. I am confused because I thought too rich would stop it from idling high. Correct me if I am wrong, but turning fuel screw in makes a leaner condition.