I would get mine tuned in and running great. I'd ride it that day and put it up and come back to it a day or 2 later and it wouldn't run for ****. I'd tune again and get it going and come back to it a few days later and it'd run like ****. Did this 4 or 5 times before I figured it out, and by figuring it out I mean my header pipe fell off. Fixed that and went with a 47.5 pilot and 150 main and it ran great. Switched to a Uni pod style filter and it was way to rich. With the Uni I had to use a 42 pilot and 145 main. So I went back to a K&N filter, air box lid mod, and the 47.5 and 150 with the fuel screw turned out from closed .75 turns and the needle clip down one slot and it runs awesome. I had forgot that I had sprayed wd 40 rust penetrant on the header nuts to free them up so I could change the exhaust gasket and well, that **** works great. The nuts freed up and backed off a little every time I rode it till the header fell down. Anyway I had tried every jet combo I could think of to get it to run right, I mean I screwed with it for about a week and a half before I "figured out" what was wrong. My neighbor has a stock warrior with a white bros e series pipe and I got his to purr in about 2 hours, completely different jets than I am running. I would highly suggest using the spring from a clicker pen on the accelerator pump, It makes a noticeable difference.